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| Company's Name | Location (County) | Date Well was Completed | Formation | Well's Name | Treated Interval | Cased or Open-hole (O-H) | Rate Prior to Treatment | Date it was treated | Rate After Treatment | Notes | ||||||
| BOPD | Rate MCFD | Prior BWPD | BOPD | MCFD | BWPD | |||||||||||
| USA | ||||||||||||||||
| RMOTC | Natrona, WY | 1978 | Wall Creek-2 | Teapot Dome 85-AX-10 | 3,014'-3,031' | Cased | 2.2 | 227 | 2.3 | 22-11-02 | 2 six months after |
455 six months after |
0.9 six months after |
Suppose to shot at 3,035'-3,054', Casing restriction, shot SWTorpedo 21' above | ||
| Morning Star | Hot Springs, WY | 2002 | Phosphoria | Ben-Rayn-33-1 | 978'-994' | Cased | 0 | 0 | 0 | 20-05-03 | 0 | 0 | 0 | Dry well, Pluged | ||
| Anderson Oil | Knox, KY | 2003 | Big Lime | Asher Land-8 | 3,360'-3,370' | O-H | NA | 12 | NA | NA | 39 | NA | Listed rates are an open flow. In line it puts 16 MCFD for last 12 months. | |||
| Merit Gas & Oil | Knox, KY | 2001 | Artemus Quadrangle | Blevins Corey #1 | 1,782'-1,790' | O-H | 0 | 0 | 0 | 20-03-04 | 0 | 0 | 0 | Tepmporary plug has moved about 130' below to the Devonian Shale and some gas has been seen | ||
| B & J Oil and Gas | Droppleman, B.H. - Heirs | 1966 | Berea | B-1 | 2,550'-2,568' | O-H | 4 | 22 | 10 | 13-08-04 | 20 | 53 | 30 | Six stroke pump was installed and pumping was slowdown from 60 BPD of Total fluid to 50 BPD to stop foaming. Two months after treatment Gas increase additional 15% from 45mcf to 53mcf. | ||
| B & J Oil and Gas | Keeley, Martin, Etal | 1966 | Berea | #2 | 2,552'-2,570' | O-H | 1 | 2 | 1,5 | 13-08-04 | 0,5 | 4 | 35 | After treatment rates will be posted as soon as they will become available | ||
| Interstate Natural Gas | Johnson | 2004 | Berea | Thelka Coal#2 | 1,470'-1,482' | Cased | NA | 1 | NA | 14-09-04 | NA | 143 | NA | All rates are open flow. A measurement was taken right before treatment and 15 minutes after the treatment. | ||
| J.D.Carty Resources, Inc, | Magoffin | 2004 | Big Lime | Floyd Arnett#1 | 2,090'-2,130' 2,160'- 2,220' | Cased | NA | 0 | NA | 13-09-04 | NA | 0 | NA | Very low reservoir pressure ~40psi. Wet. After first shot 600' of water has been taken by the formation and 4 hours late 500' of water did came back. No signs of improvements. | ||
| Interstate Natural Gas | Martin | 2004 | Big Lime and Berea | Dollie Cline#1 | 2,092'-2,124' 2,620'-2,640' | O-H | NA | 10 | NA | 14-10-04 | NA | 15 | NA | After shooting Berea gas show throw 1,100' of water and 100' of water was taken by the formation. Asumptions are that presure increased from 180psi to ~550psi Rate will be posted as soon as they will become available | ||
| Interstate Natural Gas | Martin | 2004 | Big Lime and Berea | Dollie Cline#2 | 2,080'-2,088' 2,100'-2,110' 2,592'-2,600' | O-H | NA | 17 | NA | 14-10-04 | NA | 23 | NA | After shooting Big Lime gas show throw 1,200' of water. Asumptions are that presure increased from 190psi to ~570psi Rate will be posted as soon as they will become available | ||
| Williams Production RMT Co. | Campbell WY | 2005 | Big George Coal Bed Methane | CORU 42-16-5075B | 1,250'-1,274' | O-H | NA | 0 | 30 | 20-04-05 | NA | 0 | 75 | After shooting Big George Coal surprisingly we found no significant coal filling in the hole and Great over 100% increase in water production as intended. | ||
| Williams Production RMT Co. | Campbell WY | 2005 | Big George Coal Bed Methane | CORU LOVE 31-21-5075B | 1,421'-1,468' | O-H | NA | 0 | 70 | 23-05-05 | NA | 0 | 117 | After shooting Big George Coal, filling of coal was 24ft all the way to the top of Torpedo head and ~70% increase in water production as intended. | ||
| Wellington Operating Company | Larimer CO | 2005 | Layns | Kiix 1 | 6,075'-6,087' | Cased | 0 | NA | NA | 20-07-05 | 25 | NA | NA | Torpedo is shoot in 2,000' of oil. 5 BOPD is registered 2 days later. | ||